Yang Zongqiao, Zhao Zengwu, Li Yongzhi, Qin Liqiang. Research on Reducing the Thickness of Decarburized Layer of High-speed Rail[J]. IRON STEEL VANADIUM TITANIUM, 2014, 35(1): 119-122. doi: 10.7513/j.issn.1004-7638.2014.01.023
Citation:
Yang Zongqiao, Zhao Zengwu, Li Yongzhi, Qin Liqiang. Research on Reducing the Thickness of Decarburized Layer of High-speed Rail[J]. IRON STEEL VANADIUM TITANIUM, 2014, 35(1): 119-122. doi: 10.7513/j.issn.1004-7638.2014.01.023
Yang Zongqiao, Zhao Zengwu, Li Yongzhi, Qin Liqiang. Research on Reducing the Thickness of Decarburized Layer of High-speed Rail[J]. IRON STEEL VANADIUM TITANIUM, 2014, 35(1): 119-122. doi: 10.7513/j.issn.1004-7638.2014.01.023
Citation:
Yang Zongqiao, Zhao Zengwu, Li Yongzhi, Qin Liqiang. Research on Reducing the Thickness of Decarburized Layer of High-speed Rail[J]. IRON STEEL VANADIUM TITANIUM, 2014, 35(1): 119-122. doi: 10.7513/j.issn.1004-7638.2014.01.023
2. Energy and the Environment Institute, Inner Mongolia University of Science and Technology, Baotou 014010, Inner Mongolia, China;
3. Key Laboratory of Integrated Exploitation of Bayan Obo Multi-metal Resources, Inner Mongolia University of Science and Technology, Baotou, 041010, Inner Mongolia, China
Based on field tests carried out during the manufacturing of high-speed steel rail in Baotou Rail and Beam Plant,effects of heating time and heating temperature on the thickness of decarburized layer of high-speed U71Mn rail are studied.Results show that in normal production,the thickness of the decarburized layer can be effectively decreased with tapping temperature of billets at 1 080~1 100℃ and uniform billet temperature.In the case of rolling delay for 15~30 min,by controlling the temperature of soaking zone and the temperature of sectionⅠof heating zone lower than 1 200℃ and 1 230℃ respectively,the production requirements can be satisfied and the thickness of the decarburized layer reduced.